I bought an 02 blaster basketcase a week and half ago. PO said it had no spark but had compression and the kick start was messed up. It came with an almost complete extra engine, new piston, rings, jug and head as well. The next day i set out to figure out the kickstart issue when I realized the engine case had been JB welded back together the whole case around starter shaft had been shattered so I moved on to the spark issue, realized the magneto flywheel was loose pulled it off and the key had sheared. New keyway and it was back together and had spark. Well to make a long story short engine ended up being swamped. case and pipe were full of water. So last weekend I built a new motor for it. Using the extra case, which was in great shape, I got I installed the new top end along with all new gaskets, pulled the carb, ripped that apart and cleaned everything on it. reinstalled everything and tried to fire nothing. No spark. Trouble shot and found the CDI was bad and replaced that today. Now have spark. Still wont run. It wants to start with a new plug on the first kick but only stumbles then nothing. pulled the plug and its wet. Gas is fresh and mixed 32/1
So far I have checked:
reeds are good, no cracks or gaps
Been thru the carb 3 times makin sure its perfectly clean and assembled properly
TORS has been disconnected at the throttle, carb and controller but not removed
oil injection is gone, all ports sealed
Nice clean white/blue spark
Keyway is in and not sheared so timing should be ok.
Although not checked with a guage compression seems excellent can't seem to find any leaks
It just seems like its get to much gas. Floats are set no gas comin out the overflow. I know Im missing something here but what. All parts I installed are stock except the CDI which is a hot shot and were installed using the manual I downloaded from this forum. I'm a noob to blasters but not mechanics. I've been wrenchin on my crap for over 20 years but this thing has me baffled. Any ideas other than using this thing as a boat anchor? Thanks for the help
So far I have checked:
reeds are good, no cracks or gaps
Been thru the carb 3 times makin sure its perfectly clean and assembled properly
TORS has been disconnected at the throttle, carb and controller but not removed
oil injection is gone, all ports sealed
Nice clean white/blue spark
Keyway is in and not sheared so timing should be ok.
Although not checked with a guage compression seems excellent can't seem to find any leaks
It just seems like its get to much gas. Floats are set no gas comin out the overflow. I know Im missing something here but what. All parts I installed are stock except the CDI which is a hot shot and were installed using the manual I downloaded from this forum. I'm a noob to blasters but not mechanics. I've been wrenchin on my crap for over 20 years but this thing has me baffled. Any ideas other than using this thing as a boat anchor? Thanks for the help