Recent content by olds68cutty

  1. olds68cutty

    Guys I need help...ladys too.

    hello all. i have a 2000 blasty with k&n filter and no air box. Also a pro circuit pipe and silencer. when i hit the throttle, it sounds like its bogging out but it will respond from accelerator cable and jump up in rpm. i am talking about quad being parked and in neutral. the main problem i am...
  2. olds68cutty

    Jetting Question

    ive been looking on the forum for more about the airbox removal. when i remove my seat i see the filter. am i removing the box under the filter? ALso the idle screw thats under the seat is attached to the microswitch on the tors system right? i removed my tors system so doesnt that remove the...
  3. olds68cutty

    Jetting Question

    Hey guys i got a question. I got a 2000 Blaster recently that came with a k&n high flow and pro circuit pipe and silencer. When i start it i open the choke and let it idle for awhile. once warm ill push in the choke and it dies ever time even when warm or hot. I recently cleaned out the carb...
  4. olds68cutty

    Need HELP!

    thanks a bunch bro. you have helped me out so much!
  5. olds68cutty

    Need HELP!

    oooppppss i meant to say should
  6. olds68cutty

    Need HELP!

    all that sounds awesome. i also have a k&n filter so im thinking ill start off with a vforce 3 reed valve and i guess keep the stock carb. ill ride like that for awhile and then probably upgrade to bigger carb and do motor work. so i get a bigger carb now for the upgraded reed valve?
  7. olds68cutty

    Need HELP!

    what would you recommend? i have a pro circuit platinum pipe and pro circuit 304 silencer. hole shot itp front and rear. everything else looks stock
  8. olds68cutty

    Need HELP!

    yea i wanna trick this baby out. start little and grow bigger. i like to feel the gains in steps
  9. olds68cutty

    Need HELP!

    lol true. ive been looking at the moose racing carb cap. so that eliminates the whole assembly i have now?
  10. olds68cutty

    Need HELP!

    sweet sounds good bro. so u think thats the problem for sure?
  11. olds68cutty

    Need HELP!

    ok so i went to turn the screw under the seat and the screw would just turn so i removed the slider assembly and removed the cover to gain access to the adjuster screw. the black plastic lip that moves the spring up and down is broken.
  12. olds68cutty

    Need HELP!

    yea orignally i had it hooked up but ill plug it back in and c what happens
  13. olds68cutty

    Need HELP!

    would the idle air screw being not adjusted right cause this problem?
  14. olds68cutty

    Need HELP!

    yea i remembered
  15. olds68cutty

    Need HELP!

    no i disconnected at the carb, the handle bar and main connector