Recent content by Manshefast

  1. M

    Blaster murders plugs and spudders at full throttle

    Have to say a stock 26mm carb will work fine try with a 240 main jet first
  2. M

    Banshee help

    No boost bottle they r junk and do nothing
  3. M

    Banshee help

    310 main jet not sure of the needle but 3rd clip stock pilot air jets and idle air screws are 2-3 turns out I was thinking it was timming
  4. M

    Banshee help

    Have good spark even changed plugs and the easy way to check for air leaks is with a can of break cleaner spray around carb boots reeds head and seals if u have a leak the motor will idle down or stall
  5. M

    Banshee help

    They put the motor in for jetting
  6. M

    Banshee help

    310 main jet not sure of the needle stock pilot air jet pilot air screws are 2-3 out. This is about five min after wormed up
  7. M

    Banshee help

    Went on first ride and was not running rite took the bike back down after five hours determined it was the exhaust packing ( it was hard as a cast) ok ran better went out for a ride three weeks ago still not running rite came home pulled the carbs and bowls ( seen moisture in the bowls) cleaned...
  8. M

    Banshee help

    Had the banshee at east coast atv in February for jetting because I had tour down the motor put on a cool head bigger rad silicone hoses and new seals put a stock air box back on with a k&n power lid( it had already t5 pipe tours eliminated toomy air filter system had a hot rods tried and...
  9. M

    Banshee help

    Long story just rebuilt this year with a 4 mil stroker has lite trail porting Cooled head timing plate so after about 5 min of runnin the rite side stops firing 2/3 -3/4 throttle ?
  10. M

    Blaster axle carrier question

    Banshee need help It's a long story 4 mill stroker cooled head timing plate runnin klutz 118 w/ SMS oil intercepter 32/1 so after about 5 min or so the rite side stopes firin ? More to it but that's the base point