Carnage from this last weekend riding. To me it looks like it was lean got hot and melted down, but i would like your opinions also. Here is a little rundown of the engine. Its a vitos 240 tripple exhaust port jug & head with the forged piston. Im also running the 3mm stuffer crank and 4 degree timing key by vitos. The exhaust is vitos fat basterd pipe and silencer. It has a pwk 35mm non air striker carb hooked to the factory reed cage with boysen reeds. Im running a k&n cone filter on the carb. I put a new clutch in it and ground the rod back flat and tappered the edge. I have the oil block off kit installed also and i premix 32:1 All the parts were brand new and the motor was built by me. Every bearing seal and retainer was replaced in the engine and transmission. Long story short i jetted it when it was about 88 degrees out and it was good plug chop confirmed. well last weekend it was 47 degrees in the morning and i did not jet for it, and i was running a br8es (hotter) instead of the recommended br9es (cooler) the result is pictured.